Another Good weekend.
Posted by admin on 22nd June 2008
Nick Good and the UK’s NG Motorsport Super Pro ET team have had time to reflect on their most successful weekend of racing yet, after the team recorded their first event win at the SPRC Summernationals. Nick writes that it was a weekend of lows, highs and a fair sprinkling of luck:
Shaun and I arrived at the track lunchtime friday, got the awning up, the car bolted together and through scrutineering. When Bob arrived in the evening we fired up the motor and set the timing and checked over the motor and trans, deciding to check the valve lash in the morning with the motor cold. Next morning, what should have been a routine check of the valve lash turned into a panic when it was discovered that #3 exhaust rocker had decided to spit out half a dozen needle rollers! It must have failed just as we had shut down the evening before as five of them were within a couple of inches of the valve spring. We popped the needle bearings back in the rocker hoping that they had all been recovered. No such luck, one was still missing! Although these bearings are only a quarter of an inch long and less than a sixteenth of an inch in diameter they are incredibly hard, so there was no way we could risk hurting the new motor. It had to be found.
First off we fished around with a magnet in the valley as best we could, then the oil came out along with the filter. No sign of it. Then the pan came off whilst the nearest valve springs were removed and checked, still nothing. Next, off with the blower and manifold and all the rockers to carefully remove and check the lifters. Bingo! The little so-and-so was sitting tight behind #1 exhaust lifter. It was popped back into the rocker to make sure it was the last one missing. Karl Harrison lent us a spare rocker, and with his assistance we started to reassemble the motor. We had obviously missed the first qualifying session but were really surprised when ten minutes into the rebuild the call for the second and only remaining session came. Doesn’t time fly when you’re enjoying yourselves! This was going to be tight. Periodic silences coming from the track gave us some hope of making it to the line.
The team of Andy, Bob, Shaun, along with invaluable help from Karl, had the motor together and fired up as the rest of the class were putting in their last runs of the day. We towed down with seconds to spare. John Everitt was last in the Super Pro queue and about to fire up. I was quickly strapped in and after a short burn out managed to stage without holding up John for too long. We had planned the first run of the day to be a half pass as we had taken some blower and timing out of the motor to concentrate on setting up the chassis, and a new rear wing with more downforce had been fitted since the last meeting. I was expecting a straight steady run to half track, no chance! Off the line then left, right and back left again to half track before coasting through the finish line. At least we were in Sunday’s race. It was only after the run that the crew told me that there just had not been time to get both rear tyres down to their correct pressures. This didn’t matter, it was a brilliant effort by all the crew to get the car to the line under real pressure.
Mechanically, Sunday was a breeze, with just between-rounds servicing and checks going as planned. Going into eliminations we had no idea what times the car would run as we only had a less than perfect half pass to work with. We guessed it would run mid 6.9s so we dialled in 7.0 so as not to leave ourselves short at the top end. It was a case of having to pull a decent light and being careful to just nose ahead at the line. This worked fine against John Everitt in round one running a 7.03. In the second round against Nigel Turner we really had some luck. The chute shook itself out at a thousand feet. There was no way I was going to catch Nigel, but fortunately for us he broke out by seven thousandths. In the third round against Bob Doyle we dropped the dial in to 6.92 and lifted to a 6.93/170.79. In the semi-final we were up against Ian Tubb who had just knocked out Simon Rowland with as close to a perfect run as you’re ever likely to see, perfect Reaction Time and four ten thousandths off his dial-in. We dropped our dial-in to 6.89. Again lifting just before the line, we ran 6.894/187.22.
The final was an anti-climax after the excitement of the previous rounds: a mix-up with Crunch’s dial in of 7.00 took away his chance in the final, which was a real shame. An easy 7.15/145 was enough to take us to our first event win.
After thinking on the Saturday that this would be a wasted weekend, we couldn’t really believe the turnaround in our fortunes on Sunday. This was a brilliant team effort, with Shaun at his first meeting as a crew member really being thrown in at the deep end. Thanks also to Karl, Rod and Kim of Team Stardust for their generous help throughout the weekend. Without the backing of our sponsors we wouldn’t be at the track, so a big Thank You to Formula Tanker Rentals, Beovax Computer Services, Focal Point Digital, Hardwick Road Garage, Chris Brown Body Repairs, BGC Motorsport Components, Glasweld Systems, D&R Engineering and Morris Armitage.
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